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Convection Mechanisms For Geothermal Heat Exchangers In A Vertical Mine ShaftBy R. Thornton
Montana Tech is located in the historic mining town of Butte, MT and is adjacent to the Orphan Boy mine. This abandoned underground mine will be the heat source for a down-hole heat exchanger (DHE)/he
Feb 27, 2013
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Navi-Drill-Welnav Combination Keeps Pilot Hole on Course at EluraBy Maynard Stenberg
Judging from the progress made in August 1989, drilling and raise boring of a 400-m (1312-ft) pilot hole at the Elura mine of Pasminco Ltd. in Southeastern Australia, an observer would never guess tha
Jan 1, 1990
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Recent Tunneling Experience Using Hydraulically Operated Haulage Systems In The German Harz MountainsBy Rolf Lange
Introduction The Harzwasserwerke, a public body of the Federal State of Lower Saxony, supplies drinking water to an area bordered by Braunschweig, Bremen, the Northern and the Western edges of the
Jan 1, 1979
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Statistical Evaluation And Discussion Of The Significance Of Naturally-Occurring Radon ExposuresBy Scott D. Thayer, George H. Milly
INTRODUCTION Ambient concentrations of radon and its daughter products have been measured and analyzed by a number of investigators for a variety of purposes. Principal among these purposes have be
Jan 1, 1981
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Sustainable Exploration for Fossil Fuel in Asturias (Spain)By P. Cienfuegos, J. Loredo, J. J. Fernández, F. Pendás
This coal basin is a fore-deep basin with a lot of similarities with the Appalachian basin in the U.S.A., where throughout the 1990s, the research in coalbed methane grew rapidly due to a combination
Jan 1, 2005
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Slurry TBM Tunnel In Rock, The Modified Detroit River Outfall No. 2By William H. Hansmire
The Modified Detroit River Outfall No. 2 (MOD DRO-2) will discharge treated wastewater to the Detroit River. Construction of a 6.4-m-diameter, 1.9-km-long tunnel was halted in 2003 by flooding during
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Enrichment of the manganese to iron ratio of ferruginous low- grade manganese ore using solid reductantBy Y. V. Swamy, B. Bhoi, H. S. Ray
Low-grade manganese ores with low Mn/Fe ratios can he enriched through selective carbon reduction of iron oxide to magnetite followed by magnetic separation o f the magnetite. Thermogravimetric ana
Jan 1, 1999
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Mobile Feeder-Beakers In High Tonnage ApplicationsBy D. M. Stephens
Feeder-Breakers were an unknown but much needed piece of machinery when U. S. underground coal mines started converting to more efficient belt haulage of the R.O.M. coal as compared to conventional me
Jan 1, 1985
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Compatibility Of Sinter/Pellet Burdens ? IntroductionBy J. O?Hanlon
The 4500 m3 blast furnace at the Redcar Works of ESC operates or, a burden of sinter and pellets, both materials being produced within the works. The early history of the furnace was given to the AIME
Jan 1, 1983
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Pilot Investigation Of High Gradient Magnetic Separation Of Oxidized Taconites ? IntroductionBy D. R. Kelland
A program has been carried out over the last two years to apply the technology of High Gradient Magnetic Separation (HGMS) to the problem of mineral beneficiation and specifically oxidized taconite ir
Jan 1, 1975
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Dragline Stripping Methods Enhanced By Explosives Casting At Bridger Coal CompanyBy M. L. Bricker
The Jim Bridger Mine is operated by Bridger Coal Company and is located in Sweetwater County, 35 miles (56 km) northeast of Rock Springs, Wyoming (USA). The general location of the mine site is shown
Jan 1, 1991
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The Commercial Readiness Of Coal Liquefaction Processes ? IntroductionBy Charles H. Rice
Coal liquefaction processes can be divided into two broad classifications - direct and indirect. Direct liquefaction processes, in general, slurry coal with a solvent and react it with hydrogen under
Jan 1, 1981
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Review Of Subsidence Control Measures - Past, Present, And Future ? 1.0 IntroductionBy Madan M. Singh
It is estimated that through 1975, there were 1.69x109 m2 (418 000 acres) of urban land threatened by potential subsidence due to mining with a value of over $12 billion (19;3 dollars; USBM, 1979). Wi
Jan 1, 1984
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Sulfide Ore Concentration And Treatment At The McCoy/Cove MineBy D. S. Kimbal
The McCoy/Cove mine is located 48 km (30 miles) south of Battle Mountain, Nevada, USA, in the Fish Creek Mountains at an elevation of 1548 m (5080 ft), see Figure 1. Joseph H. McCoy first discovered g
Jan 1, 1993
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Production Of Self-Fluxing Pellets And Their Effects On Blast Furnace Operations At Kobe Steel's Nadahama WorksBy F. Shigeyoshi
The development of pelletizing during the last ten years has continued, however, self-fluxing pellets have not been regularly and commercially produced for use in blast furnaces, except as Kobe Steel,
Jan 1, 1969
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Coal/Oil Slurry Stability Concepts - IntroductionBy W. C. Meyer
The concept of using powdered coal-in-oil-mixtures (COM) as a composite fuel to conserve oil resources and relieve import supply problems is being vigorously promoted by the Department of Energy via t
Jan 1, 1981
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Column Flotation of Eastern Oil ShalesBy C. W. Schultz
The Mineral Resources Institute at The University of Alabama is engaged in a program whose objective is to develop a beneficiation system for Eastern oil shales. Prior experience (1,2) at The Universi
Jan 1, 1989
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The Henderson Coarse Ore Conveying System-A Review of Commissioning, Start-Up, and OperationBy Walter Küng
The Henderson Coarse Ore Conveying System is a three flight belt conveyor system transporting primary crushed molybdenum ore 24 km (15 miles) underneath the North American Continental Divide. One of t
Jan 1, 2004
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Solving Industrial Mineral Flotation Problems At The Mines Branch, Ottawa, CanadaBy R. A. Wyman
"The froth flotation process was patented by E.L. Sulman, H.F.K. Pickard, and John Ballot in 1906 . . . . . . . . . .James M. Hyde installed the first froth flotation process in the U.S., about August
Jan 1, 1971
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Specifying and Acquiring Longwall Shield SupportsBy John Matthews
During 1982 and 1983, it became increasingly clear that North River No. 1 Mine would have to buy a set of replacement longwall shields. Despite extensive efforts to make improvements, the shields that
Jan 1, 1986