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Recovery of Gold by Resin-In-Pulp at the Golden Jubilee MineTwo pilot-plant investigations were conducted in which strong-base resins were compared with activated carbon for the extraction of gold cyanide from leached pulp from the Golden Jubilee Mine. The res
Jan 1, 1989
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Process and Engineering Considerations in the Pressure Leaching of Copper Refinery SlimesBy James E. Hoffmann
Oxidative pressure leaching is gradually supplanting other techniques for the decopperizing of slimes. The reasons for this include: much more rapid reactions, more compact equipment, a reduced enviro
Jan 1, 2000
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Kennecott Utah Copper Smelter Modernization (8900290e-0a5a-4331-88e1-53de0cc3185e)By C. J. Newman
Prior to 1995, the smelting process at the Kennecott Utah Copper Corporation (KUCC) smelter consisted of Noranda reactors and Pierce-Smith converters. In the consideration of expansion opportunities,
Jan 1, 1998
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Electric Sulfide Smelting Technology Elxem Engineering Division's New Processing/Design. Concept For The '80sBy Jan A. Aune
The paper describes a number of electric furnace equipment modules especially developed or modified for slag furnace applications. Both the resulting design concept for a modern electric sulfide smelt
Jan 1, 1983
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Application Of Mechanical Alloying Processing To The Formation Of Copper-Carbide AlloysBy V. Vergara
Four copper composites were obtained by mechanical alloying, using as dispersed phases of four carbide powders; they were: boron carbide, chromium carbide, silicon carbide and zirconium carbide. The p
Jan 1, 1999
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Inducarb - A New Reducing Facility For Various Oxidic Melts - IntroductionBy Antrekowitsch Jürgen
The recycling of residues from metal producing by-products has become a main field of interest in metallurgical investigations. Forced by a stricter environmental legislation and the resulting increas
Jan 1, 2006
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Performance of Carbon-Magnesia Refractories as Interpreted by MicrostructureBy T. S. Montgomery
The performance of carbon-magnesia brick in electric arc furnaces (EAF) is interpreted in light of their observed optical microstructures. Features at the bricks' hot faces were protruding pericl
Jan 1, 1982
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The Behavior Of Nd-Fe-B Magnet After N2 TreatmentsBy J. Tang
The major problem with the Nd-Fe-B magnet is its low operating temperature, i.e., the coercivity decreases so rapidly with increasing temperature that the practical maximum operating temperature-is on
Jan 1, 1992
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The Steps Required to Meet Production Targets at PT TNCO, Indonesia: A New Innovative Business StrategyBy Chris Doyle
From 1997-2000. PT INCO undertook the Fourth Line Expansion Project (FLEX) to increase annual production rates from 90-100 to 150 Mlbs Ni/year (68,000 MT Ni/yr). In 2003, PT INCO nickel production und
Jan 1, 2004
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Solidification and Electrolysis of Copper Anodes Containing Nickel, Arsenic, Antimony and BismuthBy Forsén. O.
In this ?paper practical solidification of anodes containing nickel, arsenic, antimony and bismuth is compared with the equilibrium? diagrams and kinetic ?factors. In order to clarify the distribution
Jan 1, 1987
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Research On The Melting Characteristics During The Recycling Process Of Q345B Steel Lf Refining Waste SlagBy De-qing Geng, Guang-liang Wu
The waste slag generated by the LF refining process of Q345B low alloy hot-rolled steel, still has some refining capabilities. If recycled, it can reduce environmental pollution, and save the economic
Jan 1, 2016
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Physical Modeling of Three-Phase Mixing in a Counter-Current Reaction Launder (CCRL) Process for Metal RefiningBy Lloyd R. Nelson
Experimental results of three-phase mixing in a physical model of a CCRL for metals refining are presented. The system was operated above a critical lower liquid height-to- width ratio (H,/W) of unity
Jan 1, 1995
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An Empirical Equation For The Recovery - Enrichment Ratio Curve (AREV Model)By M. A. Vera
This paper proposes a simple two-parameter model for the typical inverse relationship between recovery and flotation concentrate grade. The model is based on the mineralogical limitations imposed by t
Jan 1, 1999
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Gas Injection through Immersed Rotary LancesBy Sergey Komarov, Manuela Diaz, Sano. Masamichi
"Mixing time, bubble behavior and absorption rate of gas injected into a liquid bath through rotary L-shaped lances have been studied by cold models with an effort to improve refining characteristics
Jan 1, 1996
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Alternating Pulsed Electrolysis For Fe-Cr Alloy Coatings Using Trivalent Chromium SolutionBy Shunsuke Yagi
A surface alloying technique was investigated using alternating pulsed electrolysis in an aqueous solution containing a single metal component for the formation of an Fe-Cr layer on an iron substrate.
Jan 1, 2006
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An Investigation Of The Reduction Of Eatery Paste (A12O3-As2O3-CaO-FeO-Fe2O3-PbO-Sb2O3-SiO2) Slags With GraphiteBy Steven Wright
The reduction of a slag produced 6om the recycling of lead batteries was studied in a kilogram scale laboratory investigation by reacting with graphite at temperatures of 1180 and 1200°C. Simultaneous
Jan 1, 1994
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The Smelting of Copper-Nickel Concentrates in an Electric FurnaceBy Roger C. Urquhart
Copper-nickel-sulphide ores mined in the Rustenburg district of South Africa are generally smelted in electric furnaces because of the high-temperature slag produced, the availability of cheap electri
Jan 1, 1976
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Study on Deeply De-magnesium Oxide from Phosphate Ores by FloatationBy Zhang Qin
Dolomite is main impurity mineral in phosphate ores. In practice of phosphate ores production, the grade of concentrates is only containing P2O5 31-32%.In this study, even the increasing of floatation
Jan 1, 2009
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Simulation on Electromagnetic Stirring Casting of Copper AlloyBy Hua-qing Li
Electromagnetic stirring process effectively improves the casting quality of metals. In this paper, the physical simulation experiment, in which the molten copper is displaced by mercury, was designed
Jan 1, 2009
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Expansion of the Rio Tinto Patino Tankhouse at HuelvoBy C. Palacios
The Plant, which was started up in April 1970, was originally designed for a capacity of 40.000 ton of cathodes per annum, using 12 sections, containing 408 cells. Since then the addition of another 8
Jan 1, 1976