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IC 6875 Sand And Gravel Excavation: Part 5: Motor-Truck Haulage, Conveyor-Belt Haulage, Pumps And Pipe Lines, Barges And Towboats, Aerial Trams - IntroductionBy J. R. Thoenen
This circular is part 5 of the third paper (entitled "Excavation") of a series summarizing the technical problems involved in the production and preparation of sand and gravel. Part 1 discussed the us
Jan 1, 1936
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The Mineral Industry Of Other Areas Of South America - Ecuador (0a33dacb-bbc5-4394-991c-3b07daf339d3)By Travis Q. Lyday
During 1983, Ecuador's gross domestic product (GDP) decreased by a reported 3.3% in real terms, the second consecutive decline in the economy after more than a decade of growth generated mainly b
Jan 1, 1985
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OFR-25-82 Land Reclamation As SculptureBy David Allen Jones
A depleted county gravel pit was rehabilitated by contracting an artist to convert it into sculpture, rather than using traditional reclamation methods. The sculptor's ideas were generally implem
Jan 1, 1981
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RI 6066 Factors Influencing The Design Of Hydraulic Backfill Systems (In Two Parts) 2. Friction-Head Losses Of Barite And Limestone Slurries During Pipeline Transport ? SummaryBy John D. Bardill
Data from extensive tests was obtained on friction-head losses of various sand slurries, composed of materials of different specific gravities and under varying transport conditions, to provide useful
Jan 1, 1962
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RI 9248 - Assessment of Experimental Longwall Recovery Rooms for Increasing Productivity and Expediting Equipment Removal OperationsBy Eric R. Bauer
The U.S. Bureau of Mines, in cooperation with a southwestern Pennsylvania coal mining company, BethEnergy Inc., Mine No. 60, Eighty-Four, PA, recently assessed the feasibility of using pre driven reco
Jan 1, 1989
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OFR-42(1)-74 Protection And Troubleshooting Of Coalmine Electrical Cables - Shuttle Car Reel Test Unit - I. IntroductionSevere whipping of shuttle car trailing cables occurs when the car stops suddenly or reverses direction. This causes cable damage, and can seriously injure personnel near the cable. FMC has contra
Jan 1, 1972
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OFR-49-85 Development Of The Hvdrotransport Boost PumpBy Leslie S. Rubin
A ventilated helical boost pump was developed that can handle varying flow rates and/or solids concentrations while operating at a single rotational speed and without computer assisted feedback contro
Jan 1, 1984
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Bulletin 229 Fifty Nine Coal Mine FiresBy G. S. Rice, J. W. Paul, M. W. VONBERNEWITZ
This bulletin abstracts and reviews essential details of reports on 59 fires in different coal mines in the United States, describes the circumstances of origin and the methods of controlling or extin
Jan 1, 1927
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RI 2074 Cooperative Petroleum Work in WyomingBy F. B. Tough, B. H. Scott
"Petroleum engineering is a comparatively new branch of engineering, with which few people, even petroleum operators and mining engineers, are thoroughly familiar. Petroleum engineers are responsible
Jan 1, 1920
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RI 8690 Recovery of Zinc and Sulfur From Sphalerite Concentrates by Reaction With Sulfuric AcidBy H. H. Dewing
The Bureau of Mines constructed a process research unit (PRU) to demonstrate new technology for extracting zinc from sphalerite concentrates. Up to 9 kg/hr of sphalerite (ZnS) concentrate was reacted
Jan 1, 1982
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OFR-34-89 Thin Wall Explosion -Proof Enclosures ? Final Report ? Executive SummaryThe works recorded in this Test Report have been performed by Rade Roncar - Electrotechnical Institute of Zagreb, SFR Yugoslavia in collaboration with Bureau of Mines. The main objective of these i
Jan 1, 1987
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RI 8520 Alternative Methods for Copper Recovery From Dump Leach LiquorsThe Bureau of Mines conducted large-scale laboratory copper ore leaching tests to enable improving copper recovery from large dump-leaching operations. This was done by comparing leaching progress whe
Jan 1, 1981
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RI 3601 Selection Of Coals For Coke Making (789ffc9c-458d-4ede-9b5c-7335b2b616f3)By Joseph D. Davis
Selection of a suitable coal or coals for the manufacture of coke of desired quality with due consideration of the purpose for which the coke is intended requires careful thought, and often it will pa
Jan 1, 1942
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OFR-22-86 Dissolution Of Galena With Ferric Chloride And NitrateBy Maurice C. Fuerstenau
The kinetics of leaching galena with ferric chloride and ferric nitrate have been examined as a function of ferric concentration, salt concentration, temperature and particle size. Diffusivity of ferr
Jan 1, 1984
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OFR-16(1)-80 Three-Dimensional Finite Element Analysis Of Crosscut And Entry Intersection Of A Double - Entry Coal MineBy M. B. Balachandra
A three-dimensional finite element analysis was performed of an instrumented section of a double-entry coal mine in order to provide a comparison between field measurements and existing analytic techn
Jan 1, 1976
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IC 8806 Citrate Process Demonstration Plant DesignBy W. I. Nissen
This Bureau of Mines report presents the design for a commercial-sized flue gas desulfurization (FGD) demonstration plant that uses the citrate process. The goal of the Bureau's citrate process i
Jan 1, 1979
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RI 4159 Concentration of Gravity Tailings from the Grasselli Deposit, Park City, UtahBy T. F. Mitchell, B. K. Shibler, J. V. Batty, W. G. Sandell, G. M. Potter
"INTRODUCTION The Park City district, situated 30 miles east of Salt Lake City, Utah, in the Wasatch Mountains, Is a well-known producer of lead, zinc, and precious metals. Nearly continuous productio
Dec 1, 1947
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RI 3467 Time Study Analyses - Progress Report 2. Quarry Haulage - IntroductionBy J. R. Thoenen
In the summer of 1937 the authors began a series of time studies of the various processes employed in the' production of crushed stone. These studies, made at quarries scattered over the eastern
Jan 1, 1939
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RI 3160 The Effect Of Oxygen On Gaseous Hydrogen Sulphide Corrosion Of Tank Steel ? IntroductionBy John M. Devine
The severe corrosion of equipment that is caused by the presence of hydrogen sulphide in oil and gas has been described in detail by several authors.5 Such corrosion, termed "low-temperature hydrogen
Jan 1, 1932
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IC 9483 - Water Well Safety BitsBy Dana C. Reinke
Water well drillers are exposed to high levels of noise while working. NIOSH researchers have found that water well drillers are exposed to levels above 85dB (A) while performing certain tasks during
Jan 9, 2005