Track Bonding

Rocky Mountain Coal Mining Institute
D. C. McKeehan
Organization:
Rocky Mountain Coal Mining Institute
Pages:
2
File Size:
93 KB
Publication Date:
Jan 1, 1923

Abstract

The importance of properly bonded rail joints has received the attention of The National Research Council, whose committee will investigate several methods now used and determine the merits of each as applied to street railways. The results of this investigation should be appreciated no less by the mining industry. Literature on the subject of bonding mine tracks agrees, as a rule, "that the work is poorly done." With present day facilities there is little excuse for inadequate track conductivity, and a job well done must be maintained in order to realize results. Many years ago The Union Pacific Coal Company installed their first haulage locomotive, and at that time used the channel pin bond for joining the rails. The system utilized 500 volts and the, relatively small current for a large amount of power, undoubtedly, contributed to the success of the system. The bonding of both rails was considered imperative in those days, while now the bonding of one, rail is considered sufficient in most instances. The recent installations utilizing 250 volts and correspondingly heavier currents required a more effective method of joining the rails for use as an electrical conductor. The company has used the arc-weld bond since its introduction in 1919. The art of electric welding found great favor for various methods of doing the work. The first arc-weld bonds were placed on the outside of they ball of the rail, but the bonds were ill-adapted to rails lighter than sixty pounds per yard, and the results were that grooved locomotive wheels or derailed cars removed the bonds. Familiarity with the process of electric welding brought forth numerous schemes for joining the rails. In one, instance the rails and splice-plates were welded together and with excellent results for a short time. Track movement and vibration finally broke the welds and the method was dis¬carded. Another scheme consisted of placing a channel pin over each end of an annealed copper wire about twenty inches long. The idea was to develop some way of using short lengths of scrap wire. The pin and wire were then welded to the base of the rail. Numerous joints made in this way are still intact, but successful welds were so exceptional that the practice was abandoned. Some of these bonds were welded to the web of the rail, with the result that practically all rails broke at the weld; however, this is our only record of broken rails with arc-welded bonds. At one time a quantity of No. 2 bare iron wire wasp available and was tried as a bond and proved very satisfactory. Two or three strands twenty inches long were used and were welded to the base of the rail. The method was cheap and effective and of some merit for light rails on temporary track. The use of iron wire was criticized because it did not give a balanced circuit; that is, one having equal carrying capacity for trolley and track circuits; and I am of the opinion that this is not always necessary. The total length of bond that is in circuit is so small that it contributes very little additional resistance to the complete circuit consisting of trolley wire, rails and bonds.
Citation

APA: D. C. McKeehan  (1923)  Track Bonding

MLA: D. C. McKeehan Track Bonding. Rocky Mountain Coal Mining Institute, 1923.

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