Evolution of SAG Mill Process Control at the Xstrata Nickel Raglan Operation

- Organization:
- Canadian Institute of Mining, Metallurgy and Petroleum
- Pages:
- 20
- File Size:
- 417 KB
- Publication Date:
- Jan 1, 2008
Abstract
"The Xstrata Nickel Raglan Concentrator, located at the northern limit of Quebec’s Nunavik region has been in operation since 1997. Originally designed to process 800,000 tonnes per year of high grade nickel ore, plant capacity is currently approaching 1,200,000 tonnes per year due to an Optimization Project (FAG to SAG conversion) in 2005 and many recent processimprovements.In 2006, the Raglan Metallurgical Group with assistance from the Xstrata Process Support group decided to make SAG control one of its priorities in order to further increase throughput and improve stability. The original primary mill control logic delivered by the Optimisation Project in 2005 consisted of a simple PID loop controlling the mill charge (bearing pressure) through feed rate changes. Due to the multivariable, non-linear and disturbance dominated nature of the SAG circuit it was quickly found that this traditional PID control strategy was not able to adequately control the mill; resulting in poor stability, frequent operator interventions and less than optimum performance.This paper describes the successful integration of advanced field systems such as mill feed image analysis (Wipfrag) and crusher gap controller (ASRi), into a multi-variable fuzzy logic SAG mill controller. The process of how a strategy for control was developed and implemented directly in the existing control system (exploiting standard system capabilities) is discussed. It is also shown how this approach has provided mill automation which is simple, robust (despite erratic feed characteristics), and delivers both an increase in throughput and a reduction of variability.INTRODUCTIONOriginally commissioned as a Fully Autogenous Grinding (FAG) circuit in 1997, preparations to convert the Katinniq Concentrator Mill to SAG had in fact commenced as early as 1999, but were halted owing to alternative process improvements which achieved up to 1Mtpa as early as 2000. Up until this time, plant process controls had remained more or less static; modifications having been limited to those required by new equipment. Primary mill process controls and related measurements were at this stage limited to:"
Citation
APA:
(2008) Evolution of SAG Mill Process Control at the Xstrata Nickel Raglan OperationMLA: Evolution of SAG Mill Process Control at the Xstrata Nickel Raglan Operation. Canadian Institute of Mining, Metallurgy and Petroleum, 2008.