Brightman Street Bridge Replacement Project (fbb13111-569c-48aa-97e7-9bb48f6ec170)

Deep Foundations Institute
Arturo Ressi di Cervia Jeffrey M. Taylor
Organization:
Deep Foundations Institute
Pages:
6
File Size:
542 KB
Publication Date:
Jan 1, 2004

Abstract

"Construction of the drilled shafts for the Brightman Street Bridge Replacement Project were not only challenging due to working over the water but were also challenged by changed soil conditions, concurrent work being performed by an adjacent contractor on the same project, environmental restrictions and severe winter conditions. A total of 36 x 8 foot (2.44m) diameter drilled shafts with 7.5 foot (2.31m) rock sockets were installed for the East and West bascule piers. This project also included Osterberg Cell load testing on two production drilled shafts at both the East and West bascule piers. The results from the load test program were used to fine tune the design of the drilled shaft rock sockets. From a constructability standpoint the reverse circulation drilling method with a pile top drill rig proved to be an excellent choice for drilling the overburden and rock sockets of the large diameter deep drilled shafts. INTRODUCTIONThe replacement Brightman Street Bridge spans the Taunton River between Fall River and Somerset in Massachusetts.The new crossing is located approximately 1500 feet (450m) upstream from the existing Brightman Street Bridge, which was built in 1908. The new mainline bridge includes nine spans totaling 1725 feet (525m). A bascule type moveable span will be located in the middle of the Taunton River and provide a 200 foot (61m) open channel centered about the 400 foot (122m) navigational channel. The bascule span, which has a span length of 409 feet (124.7m), will be a trunnion-type four leaf structure with a solid deck. A site plan is shown in Figure 1 Contract 3, which includes construction of the foundations for the East and West bascule piers, was bid on December 19, 2000 and was awarded to Modern Continental Construction Company (MCC) on January 24, 2001. MCC in turn awarded the subcontract for the installation of the drilled shafts to TREVIICOS Corporation, which started mobilizing in June of 2001.The scope of work for the drilled shafts of Contract 3 consisted in installing 18 drilled shafts in three rows on each side of the river to support the bascule piers located in the middle of the Taunton River.The foundation plan for the bascule span is shown in Figure 2."
Citation

APA: Arturo Ressi di Cervia Jeffrey M. Taylor  (2004)  Brightman Street Bridge Replacement Project (fbb13111-569c-48aa-97e7-9bb48f6ec170)

MLA: Arturo Ressi di Cervia Jeffrey M. Taylor Brightman Street Bridge Replacement Project (fbb13111-569c-48aa-97e7-9bb48f6ec170). Deep Foundations Institute, 2004.

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